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The Analysis and Countermeasure of AC Filter Abnormal Switching in Xi-Zhe HVDC Project |
Ai Hongjie1, Wang Yatao1, Xiong Fei1, Jin Hongjie2, Wang Yong2 |
1. XJ Electric Corp. Ltd, Xuchang, He’nan 461000; 2. The First company of China Eighth Engineering Bureau, Ltd, Zhengzhou 450000 |
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Abstract AC filter can provide reactive power and harmonics in HVDC transmission project, which can ensure the normal starting and stopping of the converter, the bus voltage stability and the power quality. In this paper, a case study is made on the investment of the AC filter in the river and the project. The reasons of the abnormal investment and the investment are analyzed. The operation of the field shows that the optimized AC filter is normal, and the system running stably and reliably.
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Published: 23 May 2017
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Cite this article: |
Ai Hongjie,Wang Yatao,Xiong Fei等. The Analysis and Countermeasure of AC Filter Abnormal Switching in Xi-Zhe HVDC Project[J]. Electrical Engineering, 2017, 18(5): 92-96.
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URL: |
http://dqjs.cesmedia.cn/EN/Y2017/V18/I5/92
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