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| Analysis on the partial discharge of the first generator stator winding in CoCa Codo Sinclair Hydropower Station in Ecuador |
| MA Wenhao1, WU Jianhui2, WANG Bogong1, FU Qiang1,3,4,5, HU Chunxiu1,3,4,5 |
1. Harbin Electric Machinery Company Limited, Harbin 150040; 2. Beijing Huake Tongan Company Limited, Beijing 100041; 3. Harbin Research Institute of Large Electrical Machinery Company Limited, Harbin 150040; 4. State Key Laboratory of Hydro-power Equipment, Harbin 150040; 5. National Engineering Research Center of Hydropower Equipment, Harbin 150040 |
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Abstract The online partial discharge (PD) of the first generator, which has been operating for two years in the CoCa Codo Sinclair (CCS) Hydropower Station in Ecuador, was larger than that of the other generators. To analyze the reasons for the excessive PD, four offline PD detection tests were conducted from 2019 to 2022. The offline detection results showed that the PD of the A-phase branch 3 in the first test was twice that of the other branches, but in the subsequent tests, the value of the A-phase branch 3 dropped to the same level of the other branches. The value of branch 4 was higher in the last three tests, but there was no significant change. On the other hand, an analysis of the overall trend of online PD from 2016 to 2019 revealed that there were periods of temporary increase and stability, as well as periods of relatively low values. The increased PD pulse data was analyzed by using the software, and it was found that the original pulse data was incomplete, which led to deviations in the analysis of the cause. The analysis results indicate that the PD value of first generator remained within an acceptable range. Moreover, its performance has been stable over time. No corona phenomenon has been found on the surface of the stator bars. Therefore, the insulation performance of the stator winding is stable and no defects.
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Received: 07 August 2025
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| Cite this article: |
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MA Wenhao,WU Jianhui,WANG Bogong等. Analysis on the partial discharge of the first generator stator winding in CoCa Codo Sinclair Hydropower Station in Ecuador[J]. Electrical Engineering, 2026, 27(6): 60-65.
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| URL: |
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https://dqjs.cesmedia.cn/EN/Y2026/V27/I6/60
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